I got some more news from my tuner today which I will share with you. Some good and some bad.
The Good
The VCT is not working yet so more horsepower to come. Most likely will see 170bhp at the wheels.
The Bad
Because the VCT is not working and I could not control my alternator from the PMW outputs I may have killed all PMW outputs in the ECU when I connected the Alternator up without control and spiked my electricals on it first start.
So I am going to get the ECU checked out by Haltech next week. Then check my VCT wiring.
No need to control the Alternator now, it has been modified with and internal regulator.
There are a few sump leaks to fix aswell, which is an engine out job but I will fix that after I get her registered. With the engine out I can also sort the engine rubber mounts.